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-   -   DIY CNC - errors in lead screw thread - Resolved (https://www.diybanter.com/metalworking/337522-diy-cnc-errors-lead-screw-thread-resolved.html)

Dennis March 19th 12 09:52 AM

DIY CNC - errors in lead screw thread - Resolved
 

I followed the advice you all gave me & checked / tightened / aligned what I
could.

Retesting the x axis gave me the following figures that I'm pretty pleased
with.

DRO Dial Gauge (all values in mm)
0 0
1.003 1
2.03 2
3.01 3
4.01 4
5.04 5
6.03 6
8.06 8
10.05 10


I cut some test holes, a rectangular cutout and some circular cutouts.
Both were within 0.05mm (~2 thou?).

I changed the cutting bit to a 2 flute 1/8" dremel router bit and got a much
much cleaner cut with little to no melting of the plastic and little burr
left on the edge.

Some pics here of rectangular cutout & circular cutouts:

http://www.youtube.com/watch?v=spB26eMLdz0
http://www.youtube.com/watch?v=KJ2cvsCfiL8


Thanks for you help, you can be assured there will be more questions to
come!



RangersSuck March 19th 12 01:37 PM

DIY CNC - errors in lead screw thread - Resolved
 
On Mar 19, 5:52*am, "Dennis" wrote:
I followed the advice you all gave me & checked / tightened / aligned what I
could.

Retesting the x axis gave me the following figures that I'm pretty pleased
with.

DRO * *Dial Gauge (all values in mm)
0 * * * *0
1.003 * *1
2.03 * * 2
3.01 * * 3
4.01 * * 4
5.04 * * 5
6.03 * * 6
8.06 * * 8
10.05 * *10

I cut some test holes, a rectangular cutout and some circular cutouts.
Both were within 0.05mm (~2 thou?).

I changed the cutting bit to a 2 flute 1/8" dremel router bit and got a much
much cleaner cut with little to no melting of the plastic and little burr
left on the edge.

Some pics here of rectangular cutout & circular cutouts:

http://www.youtube.com/watch?v=spB26...?v=KJ2cvsCfiL8

Thanks for you help, you can be assured there will be more questions to
come!



What did you find to be the major source of error, or did you just
take the shotgun approach?

Bob La Londe[_2_] March 19th 12 07:59 PM

DIY CNC - errors in lead screw thread - Resolved
 
"rangerssuck" wrote in message
...
On Mar 19, 5:52 am, "Dennis" wrote:
I followed the advice you all gave me & checked / tightened / aligned
what I
could.

Retesting the x axis gave me the following figures that I'm pretty
pleased
with.

DRO Dial Gauge (all values in mm)
0 0
1.003 1
2.03 2
3.01 3
4.01 4
5.04 5
6.03 6
8.06 8
10.05 10

I cut some test holes, a rectangular cutout and some circular cutouts.
Both were within 0.05mm (~2 thou?).

I changed the cutting bit to a 2 flute 1/8" dremel router bit and got a
much
much cleaner cut with little to no melting of the plastic and little burr
left on the edge.

Some pics here of rectangular cutout & circular cutouts:

http://www.youtube.com/watch?v=spB26...?v=KJ2cvsCfiL8

Thanks for you help, you can be assured there will be more questions to
come!



What did you find to be the major source of error, or did you just
take the shotgun approach?



LOL. I usually do both. Try to find the major problem, and as long as I am
adjusting I adjust everything.




Dennis March 20th 12 01:12 AM

DIY CNC - errors in lead screw thread - Resolved
 

"Bob La Londe" wrote in message
...
"rangerssuck" wrote in message
...
On Mar 19, 5:52 am, "Dennis" wrote:
I followed the advice you all gave me & checked / tightened / aligned
what I
could.

Retesting the x axis gave me the following figures that I'm pretty
pleased
with.

DRO Dial Gauge (all values in mm)
0 0
1.003 1
2.03 2
3.01 3
4.01 4
5.04 5
6.03 6
8.06 8
10.05 10

I cut some test holes, a rectangular cutout and some circular cutouts.
Both were within 0.05mm (~2 thou?).

I changed the cutting bit to a 2 flute 1/8" dremel router bit and got a
much
much cleaner cut with little to no melting of the plastic and little
burr
left on the edge.

Some pics here of rectangular cutout & circular cutouts:

http://www.youtube.com/watch?v=spB26...?v=KJ2cvsCfiL8

Thanks for you help, you can be assured there will be more questions to
come!



What did you find to be the major source of error, or did you just
take the shotgun approach?



LOL. I usually do both. Try to find the major problem, and as long as I
am adjusting I adjust everything.




Shotgun approach - tightened & centred everything I could think of.

I still need to square everything up some more. Typical runout seems to be
about 0.15mm per 100mm travel on the table - probably not a major issue for
routing work.






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