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-   -   Cooling Off period (https://www.diybanter.com/metalworking/592441-cooling-off-period.html)

Terry Coombs[_2_] June 24th 17 09:18 PM

Cooling Off period
 
Well , I got the bush hog pivot bracket repaired , and it's cooling
slowly . I'm not sure just how hot it got , my IR thermometer wouldn't
read it . Not red hot , but not far off either . Welded it with some
7018 then put the heat back on it for another 20 minutes to be sure it
was uniformly hot , then packed it in firebricks and fiberglass
insulation to cool slowly . I did a check for distortion , I have a slug
that was a just-slightly-loose fit that dropped thru quite nicely . I
did contact the guy before I welded it together to ask about the pin it
rides on , he said the pin is not worn at all .

--

Snag


Ed Huntress June 24th 17 10:55 PM

Cooling Off period
 
On Sat, 24 Jun 2017 15:18:10 -0500, Terry Coombs
wrote:

Well , I got the bush hog pivot bracket repaired , and it's cooling
slowly . I'm not sure just how hot it got , my IR thermometer wouldn't
read it . Not red hot , but not far off either . Welded it with some
7018 then put the heat back on it for another 20 minutes to be sure it
was uniformly hot , then packed it in firebricks and fiberglass
insulation to cool slowly . I did a check for distortion , I have a slug
that was a just-slightly-loose fit that dropped thru quite nicely . I
did contact the guy before I welded it together to ask about the pin it
rides on , he said the pin is not worn at all .

--

Snag


Let's hope it holds together. I'll bet it will be perfectly fine.

Although there is an entire mythology about welding 4130, it's really
relatively ductile, which makes it more forgiving that many people
think.

As I said in that article, the reason 4130 leads to so much
head-scratching is that it's *very* slow-quenching. In thin tubes,
which are almost always welded in the normalized condition, it can
wind up quench-hardened from welding. It actually will air-harden.
That's why it was two decades before TIG welding it was accepted. It's
only recently (the last couple of decades) that MIG welding has met
the approval of the "experts." Stick is similar.

Sections as thick as you're welding generally don't experience that
quench-hardening problem, but the quench characteristics can produce a
very confused HAZ. That's why the pre-heating and the slow cooling.
Every authority I've talked to over the last decade or so says that's
all it takes.

--
Ed Huntress

[email protected] June 25th 17 12:56 AM

Cooling Off period
 
On Sat, 24 Jun 2017 17:55:20 -0400, Ed Huntress
wrote:

On Sat, 24 Jun 2017 15:18:10 -0500, Terry Coombs
wrote:

Well , I got the bush hog pivot bracket repaired , and it's cooling
slowly . I'm not sure just how hot it got , my IR thermometer wouldn't
read it . Not red hot , but not far off either . Welded it with some
7018 then put the heat back on it for another 20 minutes to be sure it
was uniformly hot , then packed it in firebricks and fiberglass
insulation to cool slowly . I did a check for distortion , I have a slug
that was a just-slightly-loose fit that dropped thru quite nicely . I
did contact the guy before I welded it together to ask about the pin it
rides on , he said the pin is not worn at all .

--

Snag


Let's hope it holds together. I'll bet it will be perfectly fine.

Although there is an entire mythology about welding 4130, it's really
relatively ductile, which makes it more forgiving that many people
think.

As I said in that article, the reason 4130 leads to so much
head-scratching is that it's *very* slow-quenching. In thin tubes,
which are almost always welded in the normalized condition, it can
wind up quench-hardened from welding. It actually will air-harden.
That's why it was two decades before TIG welding it was accepted. It's
only recently (the last couple of decades) that MIG welding has met
the approval of the "experts." Stick is similar.

Sections as thick as you're welding generally don't experience that
quench-hardening problem, but the quench characteristics can produce a
very confused HAZ. That's why the pre-heating and the slow cooling.
Every authority I've talked to over the last decade or so says that's
all it takes.

When welding thin normalized or annealed 4130 that will not be heat
treated, using a mild steel filler "draws" some of the carbon and
alloy from the base into the weldment, making the air hardening/quench
hardening less of a problem, and as the weld is generally thicker than
the tubing being welded, the lesser tensile strength of the weldment
is not an issue, as there is more metal, of lower strength, producing
virtually the same(or better) strength overall, and the joint/HAZ is
slightly softer, more ductile, or less brittle.

Gunner Asch[_6_] June 25th 17 08:09 AM

Cooling Off period
 
On Sat, 24 Jun 2017 19:56:30 -0400, wrote:

On Sat, 24 Jun 2017 17:55:20 -0400, Ed Huntress
wrote:

On Sat, 24 Jun 2017 15:18:10 -0500, Terry Coombs
wrote:

Well , I got the bush hog pivot bracket repaired , and it's cooling
slowly . I'm not sure just how hot it got , my IR thermometer wouldn't
read it . Not red hot , but not far off either . Welded it with some
7018 then put the heat back on it for another 20 minutes to be sure it
was uniformly hot , then packed it in firebricks and fiberglass
insulation to cool slowly . I did a check for distortion , I have a slug
that was a just-slightly-loose fit that dropped thru quite nicely . I
did contact the guy before I welded it together to ask about the pin it
rides on , he said the pin is not worn at all .

--

Snag


Let's hope it holds together. I'll bet it will be perfectly fine.

Although there is an entire mythology about welding 4130, it's really
relatively ductile, which makes it more forgiving that many people
think.

As I said in that article, the reason 4130 leads to so much
head-scratching is that it's *very* slow-quenching. In thin tubes,
which are almost always welded in the normalized condition, it can
wind up quench-hardened from welding. It actually will air-harden.
That's why it was two decades before TIG welding it was accepted. It's
only recently (the last couple of decades) that MIG welding has met
the approval of the "experts." Stick is similar.

Sections as thick as you're welding generally don't experience that
quench-hardening problem, but the quench characteristics can produce a
very confused HAZ. That's why the pre-heating and the slow cooling.
Every authority I've talked to over the last decade or so says that's
all it takes.

When welding thin normalized or annealed 4130 that will not be heat
treated, using a mild steel filler "draws" some of the carbon and
alloy from the base into the weldment, making the air hardening/quench
hardening less of a problem, and as the weld is generally thicker than
the tubing being welded, the lesser tensile strength of the weldment
is not an issue, as there is more metal, of lower strength, producing
virtually the same(or better) strength overall, and the joint/HAZ is
slightly softer, more ductile, or less brittle.


Ayup.

---
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