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Bob La Londe[_2_] December 15th 11 08:49 PM

Washer Guide - Home Shop Machinist
 
I just received an email from HSM where one guy improved the accuracy,
runout, deflection of his inexpensive drill press by bolting a snug fitting
washer to the top of his quill that rides inside the column against the
sides.

My first thought was, "Won't that introduce wear to the inside of the
column?" My second was, "Gee that does sound like it work work if you used
a softer sacrificial material fro your washer/spacer."

Not that I am convinced I want to do this to my drill presses, but I you
were to take this approach with the thought that you might want to use these
everyday. Not just once in a while what would you make that washer out of?

************* Text of email received *************
Improving Drill Press Accuracy
By Quincy Collins
Many budget-priced drill presses have a fair amount of runout, or play,
especially as the quill is extended. Mine is no exception, so I headed to
the internet to try to find a solution. The bulletin boards seemed to be
filled with owners unhappy with the accuracy of their drill presses.

Some suggested flattening the splines with a hammer to reduce play, which
seemed a little drastic to me. I then hit on this solution that has worked
for me and is a little more elegant than taking a hammer to the drill press.

The upper end of my quill, where it passes through the pulleys, had a
countersunk center mark. I simply drilled and tapped this location and used
a screw to attach a custom washer (Figure 1). The washer was sized on the
lathe for a close tolerance with the bore of the pulley shaft. This served
to stabilize the quill at all points in its travel.

The spindle runout of my drill press has been greatly reduced and drilling
is now a much happier and less frustrating job. I have limited shop time so
it was nice to have found a solution that was both quick and easy.

Thanks Quincy, your subscription has been extended by an issue!
*************






[email protected] December 15th 11 10:12 PM

Washer Guide - Home Shop Machinist
 
On Dec 15, 3:49*pm, "Bob La Londe" wrote:
I just received an email from HSM where one guy improved the accuracy,
runout, deflection of his inexpensive drill press by bolting a snug fitting
washer to the top of his quill that rides inside the column against the
sides.

My first thought was, "Won't that introduce wear to the inside of the
column?" *My second was, "Gee that does sound like it work work if you used
a softer sacrificial material fro your washer/spacer."

Not that I am convinced I want to do this to my drill presses, but I you
were to take this approach with the thought that you might want to use these
everyday. *Not just once in a while what would you make that washer out of?



My first thought was teflon, but I think a better choice would be
UHMW. MSC sells it.

Dan

Lloyd E. Sponenburgh[_3_] December 15th 11 10:43 PM

Washer Guide - Home Shop Machinist
 
" fired this volley in news:4a3aa825-
:

My first thought was teflon, but I think a better choice would be
UHMW


Ultra high molecular weight WHAT? You mean, "Polyethylene"?

For lubricity, you might want to use extreme-temperature PTFE. Weird stuff
to cut, but it wears almost forever in a metal bore, and produces about
1/10th the friction coefficient of UHMW-PE.

LLoyd

Tom Gardner[_6_] December 15th 11 11:33 PM

Washer Guide - Home Shop Machinist
 
On 12/15/2011 3:49 PM, Bob La Londe wrote:
I just received an email from HSM where one guy improved the accuracy,
runout, deflection of his inexpensive drill press by bolting a snug
fitting washer to the top of his quill that rides inside the column
against the sides.

My first thought was, "Won't that introduce wear to the inside of the
column?" My second was, "Gee that does sound like it work work if you
used a softer sacrificial material fro your washer/spacer."

Not that I am convinced I want to do this to my drill presses, but I you
were to take this approach with the thought that you might want to use
these everyday. Not just once in a while what would you make that washer
out of?
////


I saw that and immediately didn't like it. It seems to me that anything
CAN be fixed right...unless you're in a hurry.

Carl Ijames December 15th 11 11:46 PM

Washer Guide - Home Shop Machinist
 
Polyethylene is definitely the cheapest choice but will cold flow under
pressure. Besides the PTFE mentioned below, which I've never worked with,
I've had good luck with Nylatron, nylon with molybdenum disulfide filler
(harder and stiffer than PE, no cold flow, machines well).

-----
Regards,
Carl Ijames
"Lloyd E. Sponenburgh" wrote in message
. 3.70...

" fired this volley in news:4a3aa825-
:

My first thought was teflon, but I think a better choice would be
UHMW


Ultra high molecular weight WHAT? You mean, "Polyethylene"?

For lubricity, you might want to use extreme-temperature PTFE. Weird stuff
to cut, but it wears almost forever in a metal bore, and produces about
1/10th the friction coefficient of UHMW-PE.

LLoyd



Bob La Londe[_2_] December 16th 11 12:36 AM

Washer Guide - Home Shop Machinist
 
"Tom Gardner" mars@tacks wrote in message
...
On 12/15/2011 3:49 PM, Bob La Londe wrote:
I just received an email from HSM where one guy improved the accuracy,
runout, deflection of his inexpensive drill press by bolting a snug
fitting washer to the top of his quill that rides inside the column
against the sides.

My first thought was, "Won't that introduce wear to the inside of the
column?" My second was, "Gee that does sound like it work work if you
used a softer sacrificial material fro your washer/spacer."

Not that I am convinced I want to do this to my drill presses, but I you
were to take this approach with the thought that you might want to use
these everyday. Not just once in a while what would you make that washer
out of?
////


I saw that and immediately didn't like it. It seems to me that anything
CAN be fixed right...unless you're in a hurry.


So how do you fix them "right". Given the premise that throw them away and
spend 10-20 times as much for a good drill press is not an option for most
folks.






Artemus[_4_] December 16th 11 01:41 AM

Washer Guide - Home Shop Machinist
 

"Bob La Londe" wrote in message
...

So how do you fix them "right". Given the premise that throw them away and
spend 10-20 times as much for a good drill press is not an option for most
folks.

Bob if you can see this (eternal sept sometimes doesn't always post
my replies to other servers - or you may have me filtered out) reply
and I'll write up the fix I did on my craftsman 15" DP #113213151.
It isn't the perfect fix but is a big improvement and is simple to do.
Art



Bob La Londe[_2_] December 16th 11 02:15 AM

Washer Guide - Home Shop Machinist
 
"Artemus" wrote in message
...

"Bob La Londe" wrote in message
...

So how do you fix them "right". Given the premise that throw them away
and
spend 10-20 times as much for a good drill press is not an option for
most
folks.

Bob if you can see this (eternal sept sometimes doesn't always post
my replies to other servers - or you may have me filtered out) reply
and I'll write up the fix I did on my craftsman 15" DP #113213151.
It isn't the perfect fix but is a big improvement and is simple to do.
Art



Hey Art,

Sure post away. I'ld love to see your fix.

Bob




Artemus[_4_] December 16th 11 02:54 AM

Washer Guide - Home Shop Machinist
 

"Bob La Londe" wrote in message
...
"Artemus" wrote in message
...

"Bob La Londe" wrote in message
...

So how do you fix them "right". Given the premise that throw them away
and
spend 10-20 times as much for a good drill press is not an option for
most
folks.

Bob if you can see this (eternal sept sometimes doesn't always post
my replies to other servers - or you may have me filtered out) reply
and I'll write up the fix I did on my craftsman 15" DP #113213151.
It isn't the perfect fix but is a big improvement and is simple to do.
Art



Hey Art,

Sure post away. I'ld love to see your fix.

Bob

Here ya go.

See diagram at
http://c.searspartsdirect.com/lis_pn...5154-00001.png
Note the screws (#28) in the lower left. The bottom one goes thru
#27 and into a threaded hole in the head. This hole is open inside the
head all the way to the quill tube. I drilled the old threads (0.8-8 metric)
in the head out and tapped with 1/4-28 threads. The head casting is
not very thick and I wanted more threads in it than 1/4-20 would give.
Next I threaded a 2" piece of 1/4" brass rod 1/4-28 for about 3/4"
on one end and 1/4-20 on the other end for this knob
http://www.rockler.com/gallery.cfm?O...lect=Detai ls.
The end that contacts the quill tube was filed flat across w/ a slight
chamfer on the corner.

To use just tighten it up so the quill play is nil but the quill still travels
up/down easily. Tighten it some more and the quill will lock to
hold the chuck at any depth.

It's been about 10 years since I've done this and it's still working just fine
with no wear on the quill at all from the brass rod .

I can post some pics tomorrow if you need them.
Art




Leon Fisk December 16th 11 08:35 PM

Washer Guide - Home Shop Machinist
 
On Thu, 15 Dec 2011 23:11:23 -0700
"Bob La Londe" wrote:

"Artemus" wrote in message
...

snip
Here ya go.

See diagram at
http://c.searspartsdirect.com/lis_pn...5154-00001.png
Note the screws (#28) in the lower left. The bottom one goes thru
#27 and into a threaded hole in the head. This hole is open inside the
head all the way to the quill tube. I drilled the old threads (0.8-8
metric)
in the head out and tapped with 1/4-28 threads. The head casting is
not very thick and I wanted more threads in it than 1/4-20 would give.
Next I threaded a 2" piece of 1/4" brass rod 1/4-28 for about 3/4"
on one end and 1/4-20 on the other end for this knob
http://www.rockler.com/gallery.cfm?O...lect=Detai ls.
The end that contacts the quill tube was filed flat across w/ a slight
chamfer on the corner.

To use just tighten it up so the quill play is nil but the quill still
travels
up/down easily. Tighten it some more and the quill will lock to
hold the chuck at any depth.

It's been about 10 years since I've done this and it's still working just
fine
with no wear on the quill at all from the brass rod .

I can post some pics tomorrow if you need them.
Art



Art, Thank you.

I've been a working all day on a part so I'm a little punchy. I'll read
your comment and look at the diagram again in the morning, but a picture is
always worth a thousand words.

Bob


Some one here posted a link to images where they did something similar
awhile back. They drilled two holes through the front casting offset at
about 90 deg and then did the same thing with some bronze/brass
inserts. The holes were in the front corners in the casting at about
the same height as your hole. It looked really tacky, but he claimed
it worked well and sounds good in theory. I've tried the one point as
you mentioned but there is still too much play. Need at least two
contact points to take out the slop in my presses...

But, the fix Bob passed on is for the spline area that slides up/down
inside the quill.

Look at this image:

http://c.searspartsdirect.com/lis_pn...5154-00003.png

Your fix takes the slop out of item: 6

Bob's fix (or what he passed on) takes the slop out of item: 11

Well... at least that is the way I see it...

--
Leon Fisk
Grand Rapids MI/Zone 5b
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