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Electronics Repair (sci.electronics.repair) Discussion of repairing electronic equipment. Topics include requests for assistance, where to obtain servicing information and parts, techniques for diagnosis and repair, and annecdotes about success, failures and problems. |
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#1
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Hi all,
I've completed my tests of the main transformer and am now 99% certain that it is the cause of all the problems I've been experiencing with this old analogue scope. It's clear there's something very wrong with the large, multi-tapped output winding. Here's the schematic again: https://www.flickr.com/photos/128859...in/dateposted- I removed ALL connections from the transformer. ALL the other output windings are giving exactly the outputs I would expect from a given input; it's just the long winding on the lower right hand side that's giving nonsense outputs. As you can see, the centre tap is grounded and there are 3 tapping points either side of it. When injected with a 20kHz sine wave of 50V p-p to the primary winding, the peak-to-peak outputs from the problem secondary at each tap are as follows (from top to bottom) 13V 13V 3V 0V (gnd) 3V 1.8V 1.8V I would have expected these voltages to be symmetrical either side of the 0V centre tap, but as you can see, this isn't the case at all. I can only conclude from this, to use a technical term, that this tranny is ****ed. If there's something obvious I've overlooked (which I doubt) please feel free to point it out. Otherwise I'll be opening it up to perform an autopsy over the weekend. Thanks again to everyone who tried to help. |
#2
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On 19.02.2016 20:20, Cursitor Doom wrote:
Hi all, I've completed my tests of the main transformer and am now 99% certain that it is the cause of all the problems I've been experiencing with this old analogue scope. It's clear there's something very wrong with the large, multi-tapped output winding. Here's the schematic again: https://www.flickr.com/photos/128859...in/dateposted- I removed ALL connections from the transformer. ALL the other output windings are giving exactly the outputs I would expect from a given input; it's just the long winding on the lower right hand side that's giving nonsense outputs. As you can see, the centre tap is grounded and there are 3 tapping points either side of it. When injected with a 20kHz sine wave of 50V p-p to the primary winding, the peak-to-peak outputs from the problem secondary at each tap are as follows (from top to bottom) 13V 13V 3V 0V (gnd) 3V 1.8V 1.8V I would have expected these voltages to be symmetrical either side of the 0V centre tap, but as you can see, this isn't the case at all. I can only conclude from this, to use a technical term, that this tranny is ****ed. If there's something obvious I've overlooked (which I doubt) please feel free to point it out. Otherwise I'll be opening it up to perform an autopsy over the weekend. Thanks again to everyone who tried to help. Hi If you had a reliable connection to the primary and all secondaries were in fact free (either the tranny completely removed from the circuit board or at least no diodes anywhere remaining), then that would mean the voltages are likely screwed up... But wait: Are you sure that you have not mixed up the windings? Maybe the two 1.8V windings are actually the 2 symmetrical "innermost" ones, the 3V ones are the "medium" ones and the 15V are the "outermost" windings? Your measured winding voltage ratios "1.8:3.0:13.0 volts" and the schematic output voltage ratios "6.7:13.4:60.7 volts" (I've added a little compensation for 0.7V silicon diodes) are (from a purely ratiometric point of view) not very far away from each other. In fact they are so close that the differences between the smaller ones can be easily explained by your measurement errors (how accurate was that 0.8V measurement anyway?) and the possibly intended uneven loading of the power rails in the scope. So, considering the winding connections slightly rearranged, the transformer looks just fine to me. But once you have it out and disconnected, please make another test: apply ca. 15V RMS to the 12.7V winding (to the one where you measured 3V) instead of to the primary. And check if any isolation looks like breaking down. Note that the 15V value contains some compensation for the fact that the power supply uses inductors after the rectifiers (and therefore the normal winding voltage is higher than the normal output voltage). That would load the transformer close to its normal condition and any breakdown should become apparent. Regards Dimitrij |
#3
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On Fri, 19 Feb 2016 22:44:08 +0100, Dimitrij Klingbeil wrote:
Are you sure that you have not mixed up the windings? Maybe the two 1.8V windings are actually the 2 symmetrical "innermost" ones, the 3V ones are the "medium" ones and the 15V are the "outermost" windings? Your measured winding voltage ratios "1.8:3.0:13.0 volts" and the schematic output voltage ratios "6.7:13.4:60.7 volts" (I've added a little compensation for 0.7V silicon diodes) are (from a purely ratiometric point of view) not very far away from each other. In fact they are so close that the differences between the smaller ones can be easily explained by your measurement errors (how accurate was that 0.8V measurement anyway?) and the possibly intended uneven loading of the power rails in the scope. I follow what you're saying, Dimitrij, but for that to be the case, the tranformer's internal wiring would have to be twisted and I can't see why they would do that. Admittedly the ground pin is in 'real life' at the far end of pinouts rather than the centre, but... well, I don't know. If you're right you must be some kind of genius, that's all I can say. So, considering the winding connections slightly rearranged, the transformer looks just fine to me. But once you have it out and disconnected, please make another test: apply ca. 15V RMS to the 12.7V winding (to the one where you measured 3V) instead of to the primary. And check if any isolation looks like breaking down. Note that the 15V value contains some compensation for the fact that the power supply uses inductors after the rectifiers (and therefore the normal winding voltage is higher than the normal output voltage). That would load the transformer close to its normal condition and any breakdown should become apparent. OK, you're the boss! I'll carry out that investigation tomorrow and report back. Maybe I can work out if the internal taps are out of sequence compared to the schematic by measuring the DC resistance of the winding at the various taps and... well you get what I mean. Intriguing idea certainly deserves to be fully explored. Many thanks. |
#4
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On Fri, 19 Feb 2016 22:44:08 +0100, Dimitrij Klingbeil wrote:
But once you have it out and disconnected, please make another test: apply ca. 15V RMS to the 12.7V winding (to the one where you measured 3V) instead of to the primary. And check if any isolation looks like breaking down. Note that the 15V value contains some compensation for the fact that the power supply uses inductors after the rectifiers (and therefore the normal winding voltage is higher than the normal output voltage). That would load the transformer close to its normal condition and any breakdown should become apparent. I did just try this a moment ago, Dimitrij, but doing this just flattens the output from the sig gen, I'm sorry to say. Hardly surprising since it's a 600ohm unit and the 12.7V tappings are 0.52ohms 'apart'! To perform this test properly I'd have to adopt the work-around suggested by another chap here who said use an audio amp to get the current up. I may well have to do this if it comes to it. The other problem is, my oscilloscope current probe is lacking a termination unit so it's readings will be meaningless and I can't use the true RMS current range on my DVM because it's probably going to be out of its bandwidth at this frequency range. ![]() |
#5
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On 21.02.2016 14:46, Cursitor Doom wrote:
On Fri, 19 Feb 2016 22:44:08 +0100, Dimitrij Klingbeil wrote: But once you have it out and disconnected, please make another test: apply ca. 15V RMS to the 12.7V winding (to the one where you measured 3V) instead of to the primary. And check if any isolation looks like breaking down. Note that the 15V value contains some compensation for the fact that the power supply uses inductors after the rectifiers (and therefore the normal winding voltage is higher than the normal output voltage). That would load the transformer close to its normal condition and any breakdown should become apparent. I did just try this a moment ago, Dimitrij, but doing this just flattens the output from the sig gen, I'm sorry to say. Hardly surprising since it's a 600ohm unit and the 12.7V tappings are 0.52ohms 'apart'! To perform this test properly I'd have to adopt the work-around suggested by another chap here who said use an audio amp to get the current up. I may well have to do this if it comes to it. The other problem is, my oscilloscope current probe is lacking a termination unit so it's readings will be meaningless and I can't use the true RMS current range on my DVM because it's probably going to be out of its bandwidth at this frequency range. ![]() Ok, there are other simpler ways to test windings under high voltage ![]() See below for a simple test circuit that would be easily doable with a few common parts and works like an IWT (impulse winding tester): http://imgur.com/2qfjhaX It needs a power supply (can be just a mains isolation transformer with rectifier and capacitor) and it's intended to show the resonance waveform on an oscilloscope at realistic rated voltage conditions. The MOSFET (any 400 or 500 V type with less than 1 Ohm Rdson) is driven with a square wave from a signal generator (frequency should be slow enough to allow the cap to recharge, some 50 to 100 Hz) and discharges a capacitor from 320 V (rectified isolated mains) into the inductor under test. Under discharge conditions the capacitor and the inductor form a resonant circuit and slowly "ring down". The resistor heats up with prolonged operation, obviously, since it has full supply voltage across it, so that's why it's rated 10W. The waveform is measured (due to the high voltages involved) with a 400 V rated 10:1 oscilloscope probe. It should give a reasonably reliable indication whether an inductor (or a transformer) is good for use at full mains voltage or not. The circuit works similarly to a commercially available IWT and it's intended to be connected to the primary of a transformer. The waveform should look like a typical IWT waveform (search for "impulse winding tester" in Google Images to see what it looks like). Here's a good looking waveform example: http://meguro.com.my/wp-content/uploads/2013/05/Impulse-applied-chart.jpg A shorted (or otherwise overloaded) coil will decay very fast or even hardly resonate at all. A good one will resonate for many cycles. A failing one with significant corona discharge may look like this: http://www.ucetech.com.cn/en/App/Tpl...ds//day_150908 /201509081505159156.jpg This test should be easy to do, and should be able to settle the question if the transformer is "shot" with reasonable confidence. As always, when working with high voltages, pay attention to safety! Regards Dimitrij |
#6
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A short that would drop the voltage on that side of the winding should drop the voltage on the other side due to coupling. Recheck everything, that's what I say.
In fact if you got a power amp that can throw some current maybe inject into the winding that is giving the low voltage and see if it steps up in the other windings. Of course heavy current, but VERY low voltage. Interestingly I just used my Phase Linear 400 Series Two as such an amp to inject a signal into, believe it or not, the SMPS transformer of a Phillips scope ! Bunch of coincidence, but of no help to you at the moment as it is a totally different model. This one kicks the voltage down to 24 VDC and then feeds the SPMS. I see no connection for a battery but I imagine it could be made to run on batteries. Wouldn't be bad to have a scope run on like two laptop batteries... Anyway, I learned to be very careful about condemning transformers. We learn by mistakes and some of us are pretty fart smellers. I hit 191 on an IQ test once, damn, how can I even be alive ? Umm, I KNOW my IQ is not that high, it was the top I hit when I went on a kick to take alot of online IQ tests. In fact my average was so good out of the about 20 of them I took, I doubt their validity. It was over 135 which is 1 % of the world so really, I doubt it. At any rate, I would take an audio amp and feed that thing until it runs. You got nothing to lose. reconnect it al and feed it from some nice maybe 100 WPC audio amp with a 10 KHz square wave or something and see what happens.. You have no current limiting now so you follow the smoke. And BTW, that hosting you're using SUCKS. It does not respond right to my zoom command and it also nags about my browser. I suggest a Dropbox account, AND USING THE /PUBLIC directory. What's more, on Dropbox all your stuff is private, no browsing nor web crawling can find it, you MUST give out the URL by using "Copy Public URL". I highly recommend it. No ads or anything at all. Point the browser and the picture shows up, download it and I can zoom like all hell. The limitation is like 2GB. You can have really high res photos there. I have had full length movies in mine. Anyway, you need better resolution to see the diode circuit symbol numbers to know which winding is which because it does not appear to have pin numbers on the transformer. |
#7
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On Fri, 19 Feb 2016 14:49:34 -0800, jurb6006 wrote:
A short that would drop the voltage on that side of the winding should drop the voltage on the other side due to coupling. Recheck everything, that's what I say. In fact if you got a power amp that can throw some current maybe inject into the winding that is giving the low voltage and see if it steps up in the other windings. Of course heavy current, but VERY low voltage. I must admit the fact that Zs on my most powerful (voltage-wise) sig gen is 600 ohms was a concern. I would ideally like to have zapped the tranny with the same voltage and current as its working conditions would expect. There's always that nagging doubt in my mind about 'what if I'd had more power to throw at it? Would that show up something useful?' Umm, I KNOW my IQ is not that high, it was the top I hit when I went on a kick to take alot of online IQ tests. In fact my average was so good out of the about 20 of them I took, I doubt their validity. It was over 135 which is 1 % of the world so really, I doubt it. One can train for an IQ test. A lot of people don't know that, though! At any rate, I would take an audio amp and feed that thing until it runs. You got nothing to lose. reconnect it al and feed it from some nice maybe 100 WPC audio amp with a 10 KHz square wave or something and see what happens. You have no current limiting now so you follow the smoke. That's a very good idea. Must admit I hadn't thought of that dodge! And BTW, that hosting you're using SUCKS. Sorry to hear that. I didn't chose Flickr (or whatever it is) I inherited it from an old Yahoo mail account. If it's that crap, I'll ditch it. |
#8
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On Fri, 19 Feb 2016 19:20:35 -0000 (UTC), Cursitor Doom
wrote: Hi all, I've completed my tests of the main transformer and am now 99% certain that it is the cause of all the problems I've been experiencing with this old analogue scope. It's clear there's something very wrong with the large, multi-tapped output winding. Here's the schematic again: https://www.flickr.com/photos/128859...in/dateposted- I removed ALL connections from the transformer. ALL the other output windings are giving exactly the outputs I would expect from a given input; it's just the long winding on the lower right hand side that's giving nonsense outputs. As you can see, the centre tap is grounded and there are 3 tapping points either side of it. When injected with a 20kHz sine wave of 50V p-p to the primary winding, the peak-to-peak outputs from the problem secondary at each tap are as follows (from top to bottom) 13V 13V 3V 0V (gnd) 3V 1.8V 1.8V I would have expected these voltages to be symmetrical either side of the 0V centre tap, but as you can see, this isn't the case at all. I can only conclude from this, to use a technical term, that this tranny is ****ed. If there's something obvious I've overlooked (which I doubt) please feel free to point it out. Otherwise I'll be opening it up to perform an autopsy over the weekend. Thanks again to everyone who tried to help. Well, at last there is a serious effort to actually record and report real measurements. However, you may be misleading yourself. Are you sure of the pin locations and their function on the transformer? They will not likely correspond to the schematic arrangement - which is arranged for functional clarity alone. The transformer pin numbers are not identified on the schematic. This is why it is much easier to make accurate winding voltage measurements when the transformer is in-circuit, connecting to easily identifiable schematic components and circuit nodes. The voltages you report would be normal if the pin functions were as listed below 13V.......60VAC 13V.......60VAC 3V........12V5 0V (gnd) 3V........12V5 1.8V......5V 1.8V......5V The nonlinearity of the ratio is due to the increasing influence of forward diode drop at lower voltage and the proportional loading effects of differing currents on rectifiers, windings and output filtering components. Recheck pin function before jumping to conclusions. RL |
#9
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On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote:
Are you sure of the pin locations and their function on the transformer? Well I *was* until Dimitrij pointed out this possibility. He changed the thread title in his follow-up so I guess you missed it. So yes, it's something I need to further investigate and I shall report back here in due course with my findings..... |
#10
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On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote:
Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... |
#11
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On Sat, 20 Feb 2016 12:55:19 -0000 (UTC), Cursitor Doom
wrote: On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... If the transformer is removed from the board, which seems to be the case, you can probe the PCB for continuity between known component leads/schematic nodes and empty PCB transformer pin lands. Using a logical physical numbering scheme (if one is not allready present on the actual transformer body), you can assign numbers to the board and the schematic, for reference. RL |
#12
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On Sat, 20 Feb 2016 09:10:13 -0500, legg wrote:
On Sat, 20 Feb 2016 12:55:19 -0000 (UTC), Cursitor Doom wrote: On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... If the transformer is removed from the board, which seems to be the case, you can probe the PCB for continuity between known component leads/schematic nodes and empty PCB transformer pin lands. Using a logical physical numbering scheme (if one is not allready present on the actual transformer body), you can assign numbers to the board and the schematic, for reference. RL I was really struggling trying to match up the pins to their particular outputs; fortunately JC has has posted the pin-outs for this transformer and saved me some brain cells (I can't afford to lose any more). Seems the voltages I'm getting are not far off what they should be after all. |
#13
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On 20.02.2016 13:55, Cursitor Doom wrote:
On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... Inductive reactance goes up with the square of the winding's nominal voltage, so you take the square roots of your impedance values. If you then take into account that the lower impedance values are strongly dominated by the DC resistance (which stays linear and does not square) and the upper one is mostly dominated by the AC reactance (which does square), the ratios seem to look just fine (well, so far as I can see, within a reasonable margin of error). But the ratios don't tell the whole story. Even if there is a winding short, all impedances will be very low (which they sort-of are, I would have expected higher values everywhere, but then 100 kHz is maybe too high, try testing at 10 kHz and see...), but the ratios between the windings would be still be mostly correct. Try to run it on higher voltage (like 15 V applied to 12.7 V secondary), and see if it pulls excessive current and warms up. That would indicate damage more clearly. Dimitrij |
#14
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On 2/20/2016 7:55 AM, Cursitor Doom wrote:
On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... The transformer secondaries go (on the left side viewed from the top of the transformer). 1.5kV 1.0kV Gap/no pin HV Common 60 60 12 12 6 6 0 As others have pointed out this PSU will not run happy without a load and I don't know what would be suitable. When I worked on these I always just left the psu connected to the scope. Lets face it, the scopes been turned on at some point with the psu connected so its not going to do much more damage and at least you will know the loading is correct. The EHT multipliers on these break down internally on these. In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? |
#15
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All noted, thank you, gentlemen. I'll have to check those tips out
tomorrow or a divorce will be in the offing. Until I report back tomorrow then, thanks... |
#16
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On 2/20/2016 11:52 AM, Cursitor Doom wrote:
All noted, thank you, gentlemen. I'll have to check those tips out tomorrow or a divorce will be in the offing. Until I report back tomorrow then, thanks... I managed to find a PM3264 PSU to try out. Unloaded it squeals as expected so I tried a makeshift load with what I had lying around, 6 x 470R 5Watt w/w resistors. You can pull one of the connectors out of the scope for a connection. (See photos) Just for fun (and I'm running this off an isolation transformer), pull V1812 and scope T2 with T1 as probe ground. you should see a nice drive waveform for a few seconds and you can check the frequency is 20KHz. Incidentally the core on L1806 on this board was loose (came apart) and also caused squealing but of a different note. If you want me to take any readings let me know, nothing too time consuming though ![]() Photos of load (It gets hot so take care) https://www.flickr.com/photos/404665.../shares/H24830 https://www.flickr.com/photos/404665.../shares/J18jga |
#17
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On Sat, 20 Feb 2016 09:36:18 -0500, JC wrote:
The transformer secondaries go (on the left side viewed from the top of the transformer). 1.5kV 1.0kV Gap/no pin HV Common 60 60 12 12 6 6 0 Well on that basis there may be nothing wrong after all. As others have pointed out this PSU will not run happy without a load and I don't know what would be suitable. When I worked on these I always just left the psu connected to the scope. Lets face it, the scopes been turned on at some point with the psu connected so its not going to do much more damage and at least you will know the loading is correct. The EHT multipliers on these break down internally on these. It's not possible to test this board with it connected to the scope. On this model, it slots inside the two main signal boards which make access under proper, full working conditions impossible. Just *another* obstacle I've faced with this repair. The EHT multiplier has been totally disconnected all through my tests except where explicitly stated otherwise. In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? I like your thinking! But no, the one nearest the bridge is a BY208-1000 alright, the other one to the side of it is a BY134. They both tested fine out of circuit. |
#18
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On 2/21/2016 8:36 AM, Cursitor Doom wrote:
On Sat, 20 Feb 2016 09:36:18 -0500, JC wrote: It's not possible to test this board with it connected to the scope. On this model, it slots inside the two main signal boards which make access under proper, full working conditions impossible. Just *another* obstacle I've faced with this repair. The EHT multiplier has been totally disconnected all through my tests except where explicitly stated otherwise. Hi, Its been some time since I worked on these but I'm pretty sure we ran these with the board out, turned round so you can get the connectors on and I guess without the HT connected. Alternately put a suitable load on the PSU. In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? I like your thinking! But no, the one nearest the bridge is a BY208-1000 alright, the other one to the side of it is a BY134. They both tested fine out of circuit. That might be one problem, the sine voltage around T1801 is 800v, your BY134 is a 600V diode. Also HV diodes can go reverse leaky, try a high ohmsmeter on it (10-20 meg range). Shouldn't be any reverse leakage. I guess you saw my next post on this? Try a load on the board before you do any more work. It will tell you if the PSU runs silent or not under load. The one I tried was screaming like heck then silent with a load. |
#19
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On Sun, 21 Feb 2016 13:36:49 -0000 (UTC), Cursitor Doom
wrote: snip In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? I like your thinking! But no, the one nearest the bridge is a BY208-1000 alright, the other one to the side of it is a BY134. They both tested fine out of circuit. The BY134 is a lower frequency part with 2uS recovery time and is probably unsuited to replacement of BY208-1000 in any of the snubber or conversion positions indicated on the schematic primary. It should be soft recovery, medium speed (200-600nS) avalanche-rated part with a minimum 800Vprv. I'd avoid the use of anything advertised as 'ultrafast' (ie UF4007), as this circuit may need a modest recovery time in order to reduce power loss and EMI, but they could be used temporarily in troubleshooting. RL |
#20
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On 20.02.2016 15:36, JC wrote:
On 2/20/2016 7:55 AM, Cursitor Doom wrote: On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... ... ... In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? Well, if that is true then beware! V1808, V1809 and V1811 are supposed to be very fast. Any slow (more than a microsecond) diode in these positions will likely cause symptoms akin to a heavy overload. Particularly V1811, if replaced with any 1N400x, is likely to render the energy recovery circuit around L1806 as good as inoperative, thereby dumping the entire energy from the switcher harmonics into R1814, which will cause it to overheat fast. Please recheck L1806 (both windings) for turn-to-turn shorts (with a signal generator), and if any of the 3 diodes (V1808, V1809, V1811) looks like it had previously been replaced (possibly improperly replaced), consider replacing all 3 of them together, using the proper parts. Use fast soft-recovery diodes rated for 1kV here. If you can't find any, use ultrafast ones. They're maybe not optimal from an EMI standpoint here, but at least they should work well enough for testing. If you can't find a BY208-1000 replacement, a MUR4100E should work. Check C1806 for dielectric breakdown. It should be able to withstand at least 500 V (or something in that ballpark). If it doesn't, replace. Don't underestimate that L1806 energy recovery circuit. Although it doesn't by itself transfer any power to the load, this supply heavily relies on it for proper resonant operation of the main transformer. It must be working properly before you can test the main transformer waveform and have any chance of making correct measurements. Besides, your description of heavy switching noise on V1806 (when you tried to measure the base drive waveform), up to the point of the waveform being unrecognizable in the noise, seems to indicate that the L1806 circuit is shorted at high frequencies. This can be a result of either a winding short in L1806 or a breakdown in one of its diodes or some of these diodes being replaced by a generic slow silicon diode. Dimitrij |
#21
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On 21.02.2016 18:27, Dimitrij Klingbeil wrote:
On 20.02.2016 15:36, JC wrote: On 2/20/2016 7:55 AM, Cursitor Doom wrote: On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... ... In one of your pictures there are a couple of diodes that look messed up (V1809 and V1811) near the bridge. They are supposed to be BY208-1000 (1000v rectifiers), I can see "40" on one, maybe 1N4007? If you can't find a BY208-1000 replacement, a MUR4100E(G) should work. Sorry, that may be physically too big to fit. A MUR1100EG or something similar should work and fit in the available space too. Dimitrij |
#22
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On 20.02.2016 13:55, Cursitor Doom wrote:
On Sat, 20 Feb 2016 01:14:09 -0500, legg wrote: Recheck pin function before jumping to conclusions. Right; now re-checked. DC measurments proved (unsurprisingly) too close together so I re-tested using 100khz instead. These are the impedances WRT ground of the output taps of the long winding in the order they actually come out of the transformer: GND, 0.17ohms, 0.17ohms, 0.26ohms, 0.28ohms, 3.7ohms, 3.8ohms. So this doesn't seem to tally up with the schematic. Or does it? I need a pint of strong coffee to kick-start my head on this one. :-/ Anyway, later... Hi As you say, this really doesn't tally up. The ratios look ok (see my other post), but the absolute values are obviously junk. After all, Ohm's law still holds, even for reactive impedances, and 60 volts divided by 3.7 Ohms is 16 amps, which would be WAY too much for a small transformer winding's magnetization current. That would indicate very heavy overload, most probably due to a short circuit inside one of the windings. But there's something that makes me distrust those impedance numbers - and that is your use of 100 kHz as the testing frequency. First of all, did you really use 100 kHz as written? Most LCR meters have 100 Hz, 1 kHz, 10 kHz and 100 kHz signals. Did you perchance use the 100 Hz one instead? 100 Hz would be so low that the inductive part might not even register properly. Second, 100 kHz is not a good choice. The reason for this is the self-resonance frequency (SRF) of your transformer. All coils and transformers in the real world are not just coils, but LC circuits. The L part is (obviously) provided by the winding itself and the C part is the stray capacitance between the wires in the winding. Being really an LC circuit, a winding has a resonance frequency, like any "true" LC circuit would have. This is called the SRF of the winding. To make matters worse, a transformer that has multiple windings wound with different geometries and wire diameters has multiple SRFs, one for each winding. Windings with few turns of loosely packed thick wire have high SRF values, while windings with many turns of densely packed thin wire will have much lower SRFs. Your particular transformer has 2 high-voltage windings for the kV outputs. They have lots of densely packed thin wire, so their SRFs will be very low. I don't know exactly how low, but I'm sure that they will be much lower than 100 kHz, and that's what makes 100 kHz an unsuitable choice for testing. If fact, if you try to operate a winding above its SRF (let's say the winding has a 20 kHz SRF and you try to apply 100 kHz), then the winding will no longer behave like an inductor, but it will behave like a capacitor instead. I know, this seems crazy, but that's how a winding behaves above its SRF. In a transformer, where there are multiple windings, there are also multiple SRFs, so at some test frequency, some windings may happen to be below their respective SRFs, while some other windings may be above their respective SRFs, depending on how you choose the test frequency. If any winding happens to be above its SRF, then it will behave like a capacitor. As you know, capacitors behave more or less like a short circuit at high frequencies, and an above-SRF winding will behave like that too. That is, it will look (from an impedance measurement) like if it was heavily overloaded or even shorted out altogether. So your 100 kHz measurements indicated very low impedances, like some winding was shorted out. But then you also have 2 high voltage windings in there, which would have been way above SRF at 100 kHz frequency, so they will effectively behave like shorted even if they were perfectly fine otherwise. At 100 kHz they're no longer inductors, they're likely just capacitors instead. Now, to test transformer winding impedances, you need to select a reasonable test frequency. It must obviously be lower than any SRF of any winding - otherwise the transformer will appear overloaded. If you don't know the SRFs' values, you can measure them out with a signal generator and an oscilloscope. But you don't need to. Normally no transformer is operated above its SRF (it would not work very well if one tried), so you can assume the normally intended frequency of operation to be a "safe" choice that is unlikely to hit SRF limits. Your transformer is probably supposed to run at something like 20 kHz in normal resonant operation, so 20 kHz should be ok. But because it has high voltage windings, it may be very close to the HV winding's SRF. Indeed Philips engineers may even have chosen to run the transformer not below, but essentially right at SRF. They may have selected the resonance capacitors for the primary in such a way that the primary (together with the resonance capacitors) would have a resonant frequency which closely matches the self-resonance of one of the high voltage windings, being just a little bit below to account for tolerances. If that's the case, you should use a lower frequency for testing impedances. Most LCR meters don't offer 20 kHz anyway, just 10 kHz and 100 kHz as "nearest neighbors". 100 kHz won't do, so use 10 kHz. That should give you realistic impedances (which you can manually multiply by 2 to get to the in-circuit conditions). Regards Dimitrij |
#23
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On Sun, 21 Feb 2016 19:36:29 +0100, Dimitrij Klingbeil wrote:
[...] First of all, did you really use 100 kHz as written? Most LCR meters have 100 Hz, 1 kHz, 10 kHz and 100 kHz signals. Did you perchance use the 100 Hz one instead? 100 Hz would be so low that the inductive part might not even register properly. Yes, definitely 100kHz. Not my preferred choice, but the only option given the meter I used which was actually a capacitor ESR meter. [SRF remarks noted] So your 100 kHz measurements indicated very low impedances, like some winding was shorted out. But then you also have 2 high voltage windings in there, which would have been way above SRF at 100 kHz frequency, so they will effectively behave like shorted even if they were perfectly fine otherwise. At 100 kHz they're no longer inductors, they're likely just capacitors instead. Very good point. I admit I never considered that possibility. Your transformer is probably supposed to run at something like 20 kHz in normal resonant operation, so 20 kHz should be ok. But because it has high voltage windings, it may be very close to the HV winding's SRF. Indeed Philips engineers may even have chosen to run the transformer not below, but essentially right at SRF. They may have selected the resonance capacitors for the primary in such a way that the primary (together with the resonance capacitors) would have a resonant frequency which closely matches the self-resonance of one of the high voltage windings, being just a little bit below to account for tolerances. If that's the case, you should use a lower frequency for testing impedances. Most LCR meters don't offer 20 kHz anyway, just 10 kHz and 100 kHz as "nearest neighbors". 100 kHz won't do, so use 10 kHz. That should give you realistic impedances (which you can manually multiply by 2 to get to the in-circuit conditions). Yes, it might be illuminating to sweep a range of frequencies and note any resonances, I can see the value of that. Unfortunately, an LCR meter is one item of test equipment I don't have, so it would have to be sig gen and scope in combination. Anyway, it's do-able. Many thanks for your observations as always. |
#24
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I should perhaps have been more specific and stated that V1811 on the
schematic is the diode that was incorrectly replaced by that lower grade part. Anyway, replacements now on order; will report back in a few days. |
#25
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![]() Quote:
windings are actually the 2 symmetrical "innermost" ones, the 3V ones are the "medium" ones and the 15V are the "outermost" windings? Your measured winding voltage ratios "1.8:3.0:13.0 volts" and the schematic output voltage ratios "6.7:13.4:60.7 volts" (I've added a little compensation for 0.7V silicon diodes) are (from a purely ratiometric point of view) not very far away from each other. In fact they are so close that the differences between the smaller ones can be easily explained by your measurement errors (how accurate was that 0.8V measurement anyway?) and the possibly intended uneven loading of the power rails in the scope. complete pcb Last edited by EdithLeman : March 16th 16 at 09:45 PM |
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